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Volumn , Issue , 1999, Pages 967-974

Reduction of unsteady stator-rotor interaction using trailing edge blowing

Author keywords

[No Author keywords available]

Indexed keywords

ACOUSTIC NOISE; AEROACOUSTICS; AERODYNAMICS; AIRCRAFT ENGINES; ENGINES; FLOW OF FLUIDS; MASS TRANSFER; NOISE ABATEMENT; SIMULATORS; TURBOFAN ENGINES;

EID: 84983189772     PISSN: None     EISSN: None     Source Type: Conference Proceeding    
DOI: 10.2514/6.1999-1952     Document Type: Conference Paper
Times cited : (5)

References (9)
  • 2
    • 0026117935 scopus 로고
    • The Effects of Jet Injection Geometry on Two-dimensional Momentumless Wakes
    • Park, W.J., and Cimbala, J.M., “The Effects of Jet Injection Geometry on Two-dimensional Momentumless Wakes,” Journal of Fluid Mechanics, Vol. 224, 29-47, 1991.
    • (1991) Journal of Fluid Mechanics , vol.224 , pp. 29-47
    • Park, W.J.1    Cimbala, J.M.2
  • 3
    • 0342281878 scopus 로고
    • Control of the Wake from a Simulated Blade by Trailing Edge Blowing
    • Lehigh University
    • Corcoran, Timothy, “Control of the Wake from a Simulated Blade by Trailing Edge Blowing,” Masters Thesis, Mechanical Engineering Department, Lehigh University, 1992.
    • (1992) Masters Thesis, Mechanical Engineering Department
    • Corcoran, T.1
  • 4
    • 0343586942 scopus 로고
    • George, “Control of the Wake from a Simulated Blade by Trailing Edge Blowing
    • Lehigh University
    • Naumann, R. George, “Control of the Wake from a Simulated Blade by Trailing Edge Blowing,” Masters Thesis, Mechanical Engineering Department, Lehigh University, 1992.
    • (1992) Masters Thesis, Mechanical Engineering Department
    • Naumann, R.1
  • 5
    • 84983112492 scopus 로고    scopus 로고
    • System and Method for Suppression Noise Produced by Rotors
    • Succi, G.P., “System and Method for Suppression Noise Produced by Rotors,” United States Patent No. 5217349, 1993.
    • United States Patent , pp. 5217349
    • Succi, G.P.1
  • 6
    • 0029159312 scopus 로고
    • Fan Noise Reduction from a Supersonic Inlet During Simulated Aircraft Approach
    • Nuckolls, W.E., and Ng, W.F. (1995) “Fan Noise Reduction from a Supersonic Inlet During Simulated Aircraft Approach,” ASME J. of Eng. For Gas Turbines and Power, Vol. 117, No. 2, 237-244.
    • (1995) ASME J. Of Eng. For Gas Turbines and Power , vol.117 , Issue.2 , pp. 237-244
    • Nuckolls, W.E.1    Ng, W.F.2
  • 7
    • 0343889650 scopus 로고    scopus 로고
    • Effect of Choking on the Aeroacoustics of an Axisymmetric Supersonic Inlet
    • Miller, K.C., and Ng, W.F. (1997) “Effect of Choking on the Aeroacoustics of an Axisymmetric Supersonic Inlet,” J. of Sound and Vibration, in press.
    • (1997) J. Of Sound and Vibration, in Press
    • Miller, K.C.1    Ng, W.F.2


* 이 정보는 Elsevier사의 SCOPUS DB에서 KISTI가 분석하여 추출한 것입니다.