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Volumn , Issue , 1999, Pages 1235-1253
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Experimental study for multi-lobed mixer high bypass exhaust systems for subsonic jet noise reduction - Part 2: Acoustic results
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Author keywords
[No Author keywords available]
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Indexed keywords
AEROACOUSTICS;
EXHAUST SYSTEMS (ENGINE);
MIXERS (MACHINERY);
NOISE ABATEMENT;
ACOUSTIC DATA;
ACOUSTIC TREATMENT;
DESIGN METHODOLOGY;
FAN NOZZLES;
FAR-FIELD;
LASER DOPPLER ANEMOMETERS;
LOW-FREQUENCY NOISE;
SUBSONIC JETS;
ACOUSTIC NOISE;
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EID: 84983112985
PISSN: None
EISSN: None
Source Type: Conference Proceeding
DOI: None Document Type: Conference Paper |
Times cited : (11)
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References (8)
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