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Volumn 51, Issue , 2014, Pages 14-23

Temporary CO2 capture shut down: Implications on low pressure steam turbine design and efficiency

Author keywords

Capture flexibility; Exhaust loss; LP steam turbine; post combustion capture; Turn up mode

Indexed keywords

CARBON DIOXIDE; COGENERATION PLANTS; COMBUSTION; EFFICIENCY; PLANT SHUTDOWNS; STEAM;

EID: 84906959515     PISSN: 18766102     EISSN: None     Source Type: Conference Proceeding    
DOI: 10.1016/j.egypro.2014.07.002     Document Type: Conference Paper
Times cited : (8)

References (7)
  • 1
    • 34547749868 scopus 로고    scopus 로고
    • Initial evaluation of the impact of post-combustion capture of carbon dioxide on supercritical pulverised coal power plant part load performance
    • Chalmers, H. and J. Gibbins, Initial evaluation of the impact of post-combustion capture of carbon dioxide on supercritical pulverised coal power plant part load performance. Fuel, 2007. 86(14): p. 2109-2123.
    • (2007) Fuel , vol.86 , Issue.14 , pp. 2109-2123
    • Chalmers, H.1    Gibbins, J.2
  • 2
    • 84870504225 scopus 로고    scopus 로고
    • Design-point and part-load considerations for natural gas combined cycle plants with post combustion capture
    • Jordal, K., et al., Design-point and part-load considerations for natural gas combined cycle plants with post combustion capture. International Journal of Greenhouse Gas Control, 2012. 11: p. 271-282.
    • (2012) International Journal of Greenhouse Gas Control , vol.11 , pp. 271-282
    • Jordal, K.1


* 이 정보는 Elsevier사의 SCOPUS DB에서 KISTI가 분석하여 추출한 것입니다.